Is any one reading this stuff or am I just wasting my time??
Friday, May 29, 2009
Is any one reading this stuff or am I just wasting my time??
Thursday, May 28, 2009
The first picture shows the tubes in place before tightening down the head. The next shows the head torqued to spec, the rocker shaft assembly installed and torqued and the tubes compressed to make a tight seal. I mentioned the fuel pump only had one seal but forgot to say the distributor had none. I also spent about 15-20 minutes digging silicone out of the block where the push rod tubes seat. I will probably have to wait until the engine is back in the car before I can remove the oil pan for cleaning and new gasket. For those not familiar with Fiat 500 engines the pan is double walled for cooling purposes. The blower fan is ducted through the space in the oil pan. I have looked in there and can see a whole bunch of wild cherry seeds, so I know it is going to take some serious probing and fishing to get them all out. When I get it off I'll post a picture showing the ducting through the bottom of the pan.
While waiting for parts for the timing chain that I was working on while waiting for parts for the differential I was working on, I started working on the rest of the engine. I cleaned the push rod tubes and stretched them to insure a tight seal when installed. This was accomplished by putting a real snug fitting socket in the end of the tube, clamping it in a vise, and pulling and wiggling it to lengthen the bellows. This was done to both ends. The seals were then put on making sure the beveled end faces away from the tube as shown in the picture to the left. The tubes were installed in the block using small amount of oil on the seals to ease them into their holes. The other picture shows them installed. The head gasket was installed over the head studs and the head was put on the studs and and allowed to settle to the tops of the tubes. After double checking that the tubes were straight in the holes, the head was tapped into place with a rubber mallet. The head nuts were placed on the studs making sure the capped nuts were under the valve cover and the open nuts on the outside of same. I think this is to prevent oil leaks from the rocker arm area down the head studs to the block. The nuts were then torqued to 24 ft. lbs. using the pattern shown in the shop manual. Although it wasn't specified, I did it in incremental steps until I reached 24 ft. lbs. The rocker arm shaft assembly was placed over its mounting studs and the nuts torqued to 14 ft. lbs. I also replaced a few gaskets while fooling around: the distributor gasket, both fuel pump gaskets---hmmm only had one gasket on it, surprise surprise.
Wednesday, May 27, 2009
Thursday, May 21, 2009
Couple more pictures of the engine. I neglected to mention the air cleaner modification. Someone decided to cut several slits in the body of the air cleaner for an unknown(to me) reason. They have since been welded shut, ground smooth and the air cleaner painted black. You can see some of the slits on the left. There was also a 5/8" hole in the side for, I guess, the same reason. It too was repaired. I began removing parts such as the starter, generator, carburetor anything that I thought could stand a good cleaning and refurbishing. Also notice in the left picture the novel spark plug looms. Add wires, pinch together, we don't need no steenking grommets! Needless to say this was also remedied and grommets were added.
Wednesday, May 20, 2009
These were taken before pressure washing, shortly after removal of the entire power train. On the right side, you can plainly see the mickey moused
1/4" studs on the exhaust. This was only the
Tuesday, May 19, 2009
You can see the engine has been lowered all the way and pulled out some. When it is completely removed you can clearly see all the ugly undercoating that was sprayed on the walls of the engine compartment. That will all have to come off as Fiat sprayed every thing body color. I think the redone engine will really stand out against Blazing Copper Metallic. It will also make it easier to finish POR-15ing the rest of the suspension. There is one area of rust on the left side that I will have to take care of also.
Monday, May 18, 2009
See, I told you . I'll repeat, no bearings were harmed during this procedure. However, they were cleaned and re-lubed as before. You can see the tape still on the axle shaft protecting the machined surface. The other pic is the re-assembled suspension and brake. I decided it was time to tackle the axle problem. After a lot of reading of the shop manual, it was clear the power train had to come out. I removed the rear motor mount after placing my Corvair engine lift under the Fiat engine. Wow, it's a pretty good fit considering. I did the cleaning, blasting, and painting stuff on the motor mount and put it aside as you will see next post.
Sunday, May 17, 2009
While still waiting for the correct front steering parts and having exhausted all the little chores in the interior, I removed the engine cover to see what could be done with it. Sometime in its past, someone tried to close the lid without releasing the prop rod. As a result the reinforcement rib was broken and the lid was torn. Someone tried to repair it by brazing but it was not doing the job. I drilled out the spot welds to remove the rib. I used an oxy-acetylene torch to melt off the brass to assess the damage. It looked like the easiest way was to cut out the damaged section and fabricate a patch panel to fit the gap. It was welded in and ground smooth, the rib welded back on and re installed on the car. The lid would now stay up without bending in the middle but has a slight hump in the center that I'll have to massage out after removing the home made hinges. Feeling cocky, I removed the front hood to align and weld several cracks in the edges. Feels like the hood and trunk were made of tissue paper. I guess they had to keep the weight down when powering a car with only 16 1/2 H.P. I don't have any pictures of these repairs but I can take some tomorrow and post in the next installment. If anyone has any comments, questions or suggestions, feel free to send them along. Night night.
These show the before and after stripping and priming the dash that was discussed in the previous post. Now it was time to do something about the seats. Neither seat would adjust back and forth. I used a rubber mallet to persuade the seat to move on the track and was finally successful in removing the passenger seat. It looked like someone else noticed this problem, the ends of the seat frame were beat all to hell with a steel hammer, maybe even a sledge. Upon looking closely, I noticed the track on the seat was bowed, the track on the floor also looked bowed but it was spot welded to the floor. The solution seemed to be to drill out the spot welds, remove the track, bead blast it to remove many coats of paint, including BLUE, and rust. I welded some bolts to the track to act as mounting studs. When the track was straightened, a light coat of black paint applied and bolted to the floor, I repeated the process on the other track. The seat was next. I used a die grinder to remove the mushroomed metal from the ends of the track, drilled out the pivots and straightened the track. The other side was done the same and the tracks installed with shoulder bolts and locking nuts to replace the factory riveted pivots. Oh yeah, they were also painted black. The seat was placed back in the car, the tracks lubed, fingers crossed and voila! They work, the seat moves back and forth very easily and it only took a day and a half. The drivers side was next and after nudging the seat loose with my trusty rubber mallet, I took a good look at the floor on that side. It had a large patch in the recessed area in the back seat? area, a patch under the seat and a patch under the outer seat rail. Unfortunately, the patches were made of ~1/8" steel plate which meant that the seat sat higher on the outside than the inside which, I assume added to the adjustment difficulties. Rather than go through the same process as I did on the right side I made the decision to replace the whole floor. The entire left side floor panel is available for around $125 and includes new seat rails already welded to it. I am probably also going to replace the passenger side(thereby wasting all the work on the seat rails on the floor) Oh well, that's the way it goes, I guess.
The last little details of the interior clean up. The hood release cable was removed, the blue paint carefully removed from the knob and the knob was polished. The cable was lubed and stored in a plastic bag for later installation. The manual throttle received the same treatment except it was just the housing, I'll have to fit a replacement knob and cable later. The chrome strip on the dash, the door sill moldings and the window weatherstrip holders were all removed, cleaned and buffed, then clear coated. The dash had holes for an older type radio, a big one for the dial and two small ones for the tuning shafts. They looked as though they were cut out with a can opener. I decided to open it up to hold a modern DIN type radio. Like I said it's my car and I can do what I want to! I also decided to remove all switches, indicator lights and other bits and pieces from the dash. There was a deep scratch in the ever so lovely BLUE paint that would take a long time to sand out so I decided to chemically strip the entire dashboard. After metal prep, de-greasing and drying, I sprayed a coat of primer on it to keep it from rusting until paint day.
Saturday, May 16, 2009
choke/starter control. Can you imagine
As I mentioned I couldn't get to the other side of the car, so I started cleaning up the interior of the car. Everything except the seats, instrument panel and door panels was spray painted blue. The pedals, gear shift lever, the choke and starter assembly, the parking brake and the door sill moldings were all a very bright shade of robins egg blue. I started removing the paint on the heater lever just to see how easily it came off. I was lucky, the paint was real brittle and flaked right off with an Exacto knife used very gingerly. I then started on the emergency brake handle. It was removed, dis assembled, bead blasted except for the plastic button in the end, and then painted black. The choke and starter lever assembly was next .I used paint remover on it after taking it apart. I discovered it was cast aluminum so off to the buffer I went. After getting a high luster on the parts they were washed with hot soapy water to remove any traces of compound and then I coated them with clear wheel coat which is a tough clear coating made for refurbishing mag wheels. After putting it back together I was very pleased with how it looked. I don't know if it is stock or not and I don't care. It's my car and I like how it looks. So there! GGGGGG. Next was the gear shift lever. It went through the same procedure as the brake handle and I also cleaned and greased the ball and ring? joint in it. I was trying to figure the best way to clean the shift knob when I started rooting around in my Corvair stash. I found a brand new walnut shift knob that had an unknown application but looked liked something I should keep 'cause it looked so neat. As I was eyeballing it, it dawned on me, that's the same shift pattern as the Bianchina. A quick call to my cousin, the "master machinist" and a new insert was made to fit in the knob and screw on the shift rod. Yay! a good day! Next up , the accelerator pedal. It was taken apart and all the kinks and bends that didn't belong there were removed. Blasting and paint, assembly and it was done. Now for the clutch and brake pedal assembly. Again, separate the parts, protect the pivoting surfaces, blast and paint the pedals. The base was again found to be cast aluminum so it got the clearcoat treatment.
Friday, May 15, 2009
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